"This 5mm square of
pattern was a mix of no less than 15 pieces of different sized ivory and
wood arranged in a specific manner. It
was barely discernible to the human eye. "
This cabinet, which was approximately 30" x 20" x
20" with a fall and small drawers inside, came to us for restoration. Inspection
showed the carcass was split in several places and the end joints had significantly
moved. Not surprisingly it was apparent that over the years it had been
repaired, sometimes well but frequently indifferently. The lock on the fall
was a replacement, a smaller till lock, and the carrying handles were cheap
modern wrought iron ones. Unusually in a cabinet of this origin, all the
inlaid surfaces except for part of the back were covered in a relatively
thick veneer. There was an immense amount of inlay missing and much of what
remained was not secure and was curling up. A great amount of the banding
was missing and the outer row had been completely removed and replaced by
veneer.
Banding
The extent of the restoration
needed made this a challenge in itself but the repair and replacement
of the banding in a cost-effective manner was daunting. The banding
was of a Tonbridge Ware type pattern enclosed between ivory and ebony
stringing. No less than 7Oft of this banding needed making up in two
different patterns! The internal pattern was only 5mm wide and the
pattern repeated itself every 5mm. This 5mm square of pattern was
a mix of no less than 15 pieces of different sized ivory and wood
arranged in a specific manner. It was barely discernible to the human
eye.
It was photographed with a digital camera and greatly enlarged. This
enabled us to see that down the length of the banding the pieces were
all of uniform width however across the banding they were alternately
single and double sized. |
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Before starting the
work we turned to the engineering trade and bought two 6" slitting
saw blades which were about 1 1/2 mm thick. These we had ground down
to 0.4mm thick. As so much banding was needed it was essential to
reduce the waste of ivory to a minimum by using the finest saw blade.
We also had a mild steel gluing jig made up. The side and top were
tightened on threads and came up on steel stops. Each 5mm x 5mm "pattern"
was made up in 12-inch lengths. After the jig was tightened the whole
was placed in a low oven (70 deg.) so the excess glue could flow freely
out of the perforated drain holes at the top and bottom of the jig.
When several lengths had been made they were side glued together and
then "bacon sliced" off and the slivers glued up between the outer
stringing. The jig proved of enormous value as everything came out
precisely to size and the banding was relatively quickly assembled. |
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Carcass
Before work could be started
on repairing and replacing the ivory inlay, the carcass had to be
repaired.
The corner joints were injected with glue and many of the wooden
pegs which had failed in shear, were replaced. Then splines were
carefully shaped precisely to fill the splits in the carcass. Several
areas where the veneer cladding was completely missing were made
good as well as those edges of the cabinet, which had been split
away.
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Ivory Inlay
All the ivory was calibrated for thickness by gluing temporarily onto
boards and passing through a thickness sander. Before any new inlay was
applied much of the existing inlay had to be removed, flattened where
necessary and the cavity cleaned out before re-laying. All the missing
motifs were cut out to size in packs of three with a Hegner saw, then
fitted; using the finest blades, three were found to be all it could handle.
Motifs, which were incomplete, were repaired. Just under 900 pieces of
ivory alone had to be cut out, fitted and applied! When completed the
missing banding already made up to length was similarly applied. All the
replacement ivory and wood had then to be scrapped down to a true surface
avoiding the old ivory motifs, which were engraved. Only then were the
replacements engraved themselves. The outer moulding was then re-worked
around the edge of the cabinet. Finally the whole piece was given a rubber
of shellac and waxed up.
Hardware
A new lock was fabricated to fit the original pin position and back plate.
We cast suitable contemporary handles and had them and the lock plate
silver-plated. The fixing of the handles presented us with a particular
difficulty. Originally the pommels would have been either of the strap
variety, bent over and nailed inside or more likely made from half round
bar and squeezed together inside the cabinet, having previously been threaded
and then hove up on a nut and the surplus cut off. We could not do this
without removing the whole inside of the cabinet. How we overcame the
problem was to make up solid pommels, cut exactly to length and bolted
inside; even this was not easy. The handles we cast without the conical
pieces on the end, thus allowing the handle ends to pass through the pommels.
The end pieces were then hove up on threads which had already been drilled
and tapped as we could not silver solder them without destroying the silver
plating.
© 2000 BAFRA
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